Diagnostic Tech: '02 Olds Aurora
A 2002 Oldsmobile Aurora was in recently with two complaints. The
headlights would dim intermittently and there was a Malfunction
Indicator Light (MIL/Check Engine Light) on. The car had the 3.5
engine and all the luxury features you would expect in any top of the
line automobile.
After spending some time trying to find a problem with the lights and
having no luck, I decided to move on to the MIL complaint and come
back to the lighting problem later. A lot of time can be spent
checking a system but when the complaint can't be verified it can
easily become time wasted. It's better to check for the cause of a
problem while the problem is present.
I pulled a P0410 trouble code from the car's engine control module.
A P0410 will set when the engine computer has commanded the AIR pump
on and the AIR valve solenoid open but does not see the O2 sensors go
lean as they should when extra air is being pumped into the exhaust.
"An AIR pump?", you ask. Yes, an AIR pump. The modern version of the
old belt driven smog pump is still alive if not well on many GM
vehicles. The AIR pump no longer needs a belt. It is an electric motor
and tucked away under the left front fender on the Aurora. The engine
computer will provide a ground to the pump motor for testing or for
normal system use. With a ground the motor should pump fresh air which
is piped to a vacuum controlled valve at each exhaust manifold. With
the vacuum control solenoid grounded by the ECM the vacuum will reach
each valve and open them, allowing the fresh air to enter the exhaust
and accelerate the catalyst operation. The fresh air entering the
exhaust as it is commanded should lower the O2 sensor voltage to a
lean condition. The lean condition should change the fuel trims. The
engine computer does monitor the voltage on the command wire to the
solenoid and will set a circuit electrical code if the voltage does
not match the command. This means that when you see a code P0410 as a
stand-alone code, you aren't likely to find an electrical problem.
One very common problem with the GM pumps is that the design of the
air intake hose allows water to be drawn into the pump housing. This
water will eventually cause the pump motor to be very hard to turn and
even freeze up. GM Technical Service Bulletin 02-06-04-024G contains
the related information. A replacement pump and an updated hose design
to prevent the water contamination are available as a kit. The part
number is 19515548. The original air intake hose filter is open to
road splash from water while driving.
The new design is covered on the inner fender side and open to the
engine compartment near the air filter housing. The install is fairly
easy. The air filter housing and inner fender liner must be removed
for access.
After finding the pump motor on this car to be water damaged and very
difficult to turn I replaced it and the hose with the update kit.
While looking for the GM TSB and part number I had noticed something
interesting. GM TSB 01-06-03-007A concerns headlamp and interior
lights dimming in cold weather. The bulletin states that a revised
alternator is available to fix complaints of headlamp dimming in cold
weather and perhaps the blower speed slowing or changing pitch
intermittently. The problem is due to intermittent low voltage. Engine
vibration may cause the alternator to lose field continuity and the
voltage regulator to reset. Now when the car owner dropped this Olds
off he did say that the alternator had been replaced at another shop
in an attempt to fix the light problem. I wasn't going to suggest yet
another replacement. What really caught my eye is that the bulletin
does go on to say that short term voltage drops with light flickers or
fluctuation is a normal condition with high electrical demand AND that
even after installing the revised alternator the car will exhibit
short voltage dips and headlamp dimming DUE TO THE AIR PUMP CYCLING.
Now just how much worse would this be if the air pump motor was water
damaged and near frozen, causing much more current draw? It looked
like the installation of the new air pump was going to help with the
light dimming problem.
As important as it is to verify a complaint before starting a
diagnostic job is verifying a repair after the work is performed.
After clearing the trouble code a short test drive was in order.
Everything appeared to work fine with no MIL on but a P0410 is a two
trip code. In other words, if the air pump failed the monitor test
during this test drive no code would be set and no MIL turned on. It
would take a second ignition cycle and test drive to set a code. The
air pump would need to fail the self test on two trips. To make things
move along better and get the most of the test drive I usually take a
scan tool along and record the ecm data.
A look at the scan tool data showed me that the air pump test had run
and had FAILED during the drive. I would have liked to include the
scan data capture in this article. You could clearly see the ecm
activate the pump and solenoid three times and three times see no lean
signal from the O2. It then gave up and logged a failure. Yes, I would
have truly liked to include that but I did a software update on that
scan tool earlier tonight not realizing it would clear the record
memory.
Back in the shop, I used the command function of the scan tool to
command the air pump on and verified the ecm could provide ground and
the pump was fully functional. If the pump was working as commanded
then the shut-off valves were the next place to check. Vacuum from the
intake manifold is piped to the vacuum solenoid. When the ecm grounds
the solenoid it opens, allowing manifold vacuum to reach the shut-off
valves. The vacuum should then open the valves allowing the fresh air
from the pump to reach the exhaust system. If the solenoid has an
electrical problem the ecm should detect that and set a related
solenoid circuit code. There was no circuit code so I used a simple
vacuum gauge to verify 18" of vacuum to the solenoid. With the engine
running and the vacuum gauge at one shut-off valve port I grounded the
solenoid and got only 5" vacuum. I blocked the other shut-off valve
port and tried it again. This time I had 18" of vacuum. The rear-most
(right side) shut-off valve was bad and losing vacuum. With the vacuum
loss, neither shut-off valve could open so no air from the pump was
reaching the exhaust.
I actually do have scan data on the test drive done after replacing
the shut-off valve. It was saved to the pc after being captured on a
different scan tool so escaped the fate of the first data capture.
You can see the O2 sensor go lean when the pump is on verifying the
system is operational.
I love my job!
Kenneth Hayes
aka Deranger
posted by Deranger at 11:26 PM
1 Comments:
Blogger Mike said...
I second Sir John's compliments!
Deranger, you have provided yet another example of what
a present-day Master Automotive Technician must do, know,
go through, research, examine, test, confirm, verify, repair,
re-test, etc ad nauseum...
You are a glowing example of what it "really takes" to fix
today's "little space shuttles" on wheels...
Folk don't realize that a DTC DOESN'T MEAN "replace this
part".
And they don't realize or appreciate the thousands of
dollars you have in training and test equipment.
Thanks again for yet another valuable post!
Mike.
PS. And thanks for the EXTRA effort you went through to
track, document and post this case!
3:26 PM EDT
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